The week that was...
What a shocker last week was.
Starts off on saturday.
Finally got the turbo parts and exhaust all back together and on the car by lunchtime Saturday. Start her up and check everything but the oil feed line from the block is leaking....and then it stripped the thread. All happened just after 12 when everything closes down.. Damn.
So Monday i go to a fitting shop and get the correct fitting (yes the other one was wrong which is why it was leaking obviously) get back and fit it and bam! No oil leak. Woo time to drive the car...until i look under the rear and notice a big pile of oil. Damn! All the expensive haldex oil had leaked out from where the controller is. Sigh. So call up and try and get a new tube of haldex but unfortunately it couldn't come in time.
Tuesday i picked up the new tube of haldex and got home. Fixed the gasket which i think must have been around the wrong way (its quite the pain in the ass to do but no excuse). Went to fill the haldex and boom! oil goes everywhere. Doing it the same way i've done it 5 other times it manages to pressurize and blow the bottom of the haldex tube out and oil goes everywhere. Nuts another bunch of expensive oil down. Call up another place for a new tube and same deal as monday. This nearly broke me.
Wednesday. Pick up the new tube and get back to the car. All goes well with putting it in this time and no hassles. Start the car and get it off the ramps and boy was it good to drive it again. Put a smile back on my face. Drove it for Thursday and Friday loving every second of it.
Saturday Morning: Heading off down south to go kart racing pulled up at the lights and as it goes green i hear this awful thunking noise. WTF? pulled off to the side of the road expecting maybe a wheels come loose or something but they are both fine. Look in the engine bay and the passenger side drive shaft has worked all the bolts loose and came off. Freaken hell. Another $110 tow home for 3km isn't fun. Get the car back in the drive way and the end of the driveshaft comes off on the road but to be expected.
Sunday. Get the car back into the garage and notice fluid leaking out strangely. Wanted to see what damage had been done got the car up on ramps and couldn't believe my eyes when i saw it. This ****ing car hates me so much. 3 Days... 3 freaken days is how long i had the car before the next major failure.
http://www.vwwatercooled.com.au/foru...vwxosnc7-2.jpg
http://www.vwwatercooled.com.au/foru...cs7cdaiu-2.jpg
My new inspection window.
http://www.vwwatercooled.com.au/foru...o2jjhwen-2.jpg
So time to rebuild the gearbox. Well at least its kinda an excuse to change over the final drive that i brought and strengthen the box but i wish i could have done it on my own accord. Not looking forward to the bill on this one. Think it may go over the turbo sigh.
Lets see if i can get this running before the dyno day :(
Wish i didn't have to eat my words... again